Lol, he's probably reading posts right now, just wishing he had said that!! But, anyways... Mike, did they get it figured out? If not, we can come down this weekend and take a look.
Sent from my iPhone using Tapatalk
Printable View
Yes it was to simple dave just hooked up the wires as the 5 wire puck and appears to be working fine. we'll know when it gets wet soon.I appreciate the offer.
How far did Matt make it on the boat before he got sick Mike? Oh and what the hell post up some pics of that beautiful ride!!
after Matt got sick i decided to check out the cam (he did not install that or any of the other things that i'll talk about) the cam which i was told was a solid roller turned out to be a used hydraulic crane cam with rust and pits on one or two of the lobes not the new cam i paid for. having solid roller lifters and valve springs on the merlin heads set up for solid rollers i'm not sure how long the motor would have last. nothing matt did was wrong but the motor was completely taken apart. I took the boat to connolly's marine. he recommended that i take the motor to todd's performance. It turned that used rod and main bearings were installed not the new clevite bearings that I paid for. The only thing that did not have to be redone was the wiring and stuff that Chris and Candace did. dave connolley removed the shaft log that was counter sunk from the bottom leaving two holes in the shaft log that were not used. I told (name not mentioned) to install them from the top the way the were. when the shaft log was removed the shaft almost hit the side where it went through the boat. when dave removed the whip strut it moved even more. dave removed the strut and aligned every thing correctly the hole were filled and bottom re- gelled. the motor was so dirty that the cylinders had marks on them just from turning it over by hand. the motor has been completely rebuilt with a new solid roller cam, lifters , new bearings and push rods. I was luckey that i had a bad feeling about the cam that we didn't have a cam card for. to be continued
Attachment 45558Attachment 45557Attachment 45556Attachment 45559[ATTACH=CONFIG]45560 Here's the progress so far. all the plumbing is complete with push lock hose and fittings, just finishing some wiring on the motor and velvet drive and adjustments to the interior. oh yea we need to run the motor set the valves hot and some misc stuff and it will be wet soon. I can't thank matt, chris ,candace, dave connolly and todd at todds performance enough. almost done
Awesome, Can't wait till she's done, Mike!!
Sent from my iPhone using Tapatalk
That really sucks to hear Mike. Yeah I had mentioned a couple times that I would have had the motor looked at but good thing you did.. Cant wait to see pics of you and the wife heading up river in it..
yea that will be soon, both tod and dave have been incredibly fair and fast and knowledgeable with their work. I heard mat was back to work if he is please let me know. the last time i talked to him he didn't sound to good so i haven't called as i didn't want to bother him.
started the motor today fired right up. only things left are final adjustment on cavitation plates, run the motor and adjust timeing and valves when hot then install the interior. the left tank is not reading but I only put in 7 gallons don't know if its stuck from sitting so long but that will be easy and not a major issue. won't be long now
Very cool boat! Do you have any pictures of her with the interior in or better pic of the windshield?
Who made the tanks? If so, IMCO installs a short sender in their tanks in order to make the driver think they have less fuel (less likely to run out). I don't think they're set a whole 7 gallons high, but who knows, many tanks are built different.
no pictures of the interior in the boat or of the windshield. the windshield was done by finney' s plastics and powder coating here in havasu the old one was shot. by the end of next week i should have photos of everything hopefully on the water. if the sending unit isn't working i think it will be a tank removal to get it out(this winter). i'll put more gas in it first. I don't know who made the tanks, i think by 84 sanger was using the aluminum tanks that are in it. I put 15 gallons in the right side and it showed 1/2 full.
The motor was run, valves adjusted and timing set everything appears to be ok . (rear sear needs minor mods to clear velvet drive) the boat is at home. Dave offered to take the boat out with me before all the interior is in to check for any issues which we'll do next Sunday hopefully, in laws will be here this week so there would not have been any boating Todd also wants to go out to pull spark plugs to check if jets need to be changed. I'm hoping to be at Parker Oct. Candace i have all that wire left over I think chris said he could use it to rewire a boat, anyways it's yours if you want it.